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https://hdl.handle.net/1822/87131
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Campo DC | Valor | Idioma |
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dc.contributor.author | Bastos, N. M. | por |
dc.contributor.author | Alves, Anabela Carvalho | por |
dc.contributor.author | Castro, F. X. | por |
dc.contributor.author | Duarte, J. | por |
dc.contributor.author | Ferreira, L. P. | por |
dc.contributor.author | Silva, F. J. G. | por |
dc.date.accessioned | 2023-10-30T11:25:39Z | - |
dc.date.available | 2023-10-30T11:25:39Z | - |
dc.date.issued | 2021-01-01 | - |
dc.identifier.issn | 2351-9789 | - |
dc.identifier.uri | https://hdl.handle.net/1822/87131 | - |
dc.description.abstract | This article discusses the reconfiguration and improvement of electronics components assembly lines through the use of Lean Thinking principles. This reconfiguration was undertaken in a project that followed the action-research methodology. There were three main distinct problems related with the outdated assembly lines. The first came from a diagnosis of the assembly line itself, where quality problems and difficulties with compliance with the takt-time were identified, as well as activities that do not added value. The second happened due to an adjustment in demand that requires a reconfiguration of the line and, the third problem, related to the integration in an existing assembly line of a new process for a product pertaining to the same family, forcing the exploitation of synergies in production of these two products. Regarding the improvement proposals, some managed to be implemented in a timely manner, others, despite not having been implemented, their impacts has been predicted. Overall, the level of scrap was reduced by 57% through the implementation of the Lean Six Sigma methodology, and the cycle time of an operation was reduced by 12,5% by eliminating non-value adding operations. Also, gains were obtained by reducing the previous occupation with the project of an assembly line segment dedicated to the new product. With this, a reduction of one employee with the integration of two workstations was achieved. | por |
dc.description.sponsorship | I would like to thank all the company's employees who made this project possible, and for the support given. This work has been supported by FCT - Fundacao para a Ciencia e Tecnologia within the R&D Units Project Scope: UIDB/00319/2020. | por |
dc.language.iso | eng | por |
dc.publisher | Elsevier Science BV | por |
dc.relation | info:eu-repo/grantAgreement/FCT/6817 - DCRRNI ID/UIDB%2F00319%2F2020/PT | por |
dc.rights | openAccess | por |
dc.subject | Automotive components | por |
dc.subject | Lean thinking | por |
dc.subject | Lean six sigma | por |
dc.subject | Reconfiguration of asssembly lines | por |
dc.subject | Automotive industry | por |
dc.title | Reconfiguration of assembly lines using lean thinking in an electronics components' manufacturer for the automotive industry | por |
dc.type | conferencePaper | por |
dc.peerreviewed | yes | por |
oaire.citationStartPage | 383 | por |
oaire.citationEndPage | 392 | por |
oaire.citationIssue | C | por |
oaire.citationVolume | 55 | por |
dc.date.updated | 2023-10-28T21:50:39Z | - |
dc.identifier.doi | 10.1016/j.promfg.2021.10.053 | por |
dc.subject.wos | Science & Technology | - |
sdum.export.identifier | 12879 | - |
sdum.journal | Procedia Manufacturing | por |
sdum.conferencePublication | FAIM 2021 | por |
sdum.bookTitle | FAIM 2021 | por |
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Ficheiros deste registo:
Ficheiro | Descrição | Tamanho | Formato | |
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2021_Bastos_et_al_PROC MANUF_NUNO BASTOS_RECONFIGURATION OF ASSEMBLY LINES.pdf | 945,91 kB | Adobe PDF | Ver/Abrir |